Disappointing Dyno Runs Today
I brought my car in for a dynotune today. The shop I went to used a Dynojet. The best I could get was 246.1 fwhp and 242.1 ft-lbs. Not bad numbers, but considering that I just got Jim@ForeignAffairs heads installed along with a 7 psi pulley, I was pretty disappointed. Last year, with a 5.5 psi pulley and my current Apexi WS catback, I ran 246.6 fwhp and 232.9 ft-lb. This was also on a Dynojet, by the way, so I should be comparing apples to apples. At least I got some gain in the torque. Maybe that explains why the car feels stronger, even though the numbers don't back it up.
The main problem seems to be the fuel delivery. I was running lean the whole time, even with S-AFC adjustments at +25% from 3000 rpm up. When we tried to go higher, the ECU couldn't deal with it and retarded the timing. The lowest that my air fuel ratio could get to was 13.5:1, which is too high. I don't know if just getting bigger injectors will help. I know Ericsol has been using a product from Split Second to control the timing, so maybe that is the way to go. There is some good news, though; it doesn't appear that I had any problems with the knock sensor.
I'm sure headers and a new Y pipe will help, but the fuel delivery seems to be a bigger issue. At this point, the additional boost from the 7 psi pulley would appear to be wasted. I'll keep you posted as I research this further.
The main problem seems to be the fuel delivery. I was running lean the whole time, even with S-AFC adjustments at +25% from 3000 rpm up. When we tried to go higher, the ECU couldn't deal with it and retarded the timing. The lowest that my air fuel ratio could get to was 13.5:1, which is too high. I don't know if just getting bigger injectors will help. I know Ericsol has been using a product from Split Second to control the timing, so maybe that is the way to go. There is some good news, though; it doesn't appear that I had any problems with the knock sensor.
I'm sure headers and a new Y pipe will help, but the fuel delivery seems to be a bigger issue. At this point, the additional boost from the 7 psi pulley would appear to be wasted. I'll keep you posted as I research this further.
- cdssolara
- SolaraGuy Street Racer
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- Joined: Sat Nov 17, 2001 5:00 pm
- Location: Clayton, CA